4.7 Article Proceedings Paper

A failure analysis of exhaust systems for naval gas turbines. Part I: Fatigue life assessment

期刊

ENGINEERING FAILURE ANALYSIS
卷 16, 期 4, 页码 1314-1323

出版社

PERGAMON-ELSEVIER SCIENCE LTD
DOI: 10.1016/j.engfailanal.2008.08.017

关键词

High temperature fatigue; Life assessment; AISI 316L stainless steel grade type; Naval gas turbines; Exhaust systems

向作者/读者索取更多资源

Cracks nucleated and propagated through the wall thickness of naval gas turbine's exhaust systems. Each exhaust system was manufactured with AISI 316L stainless steel grade type, supplied in the annealed condition and rolled in plates with 3.8 mm thickness, which were bent and welded by MIG/MAG weld process. The main cracks propagated, along the circumferential direction, from the weld toe of some butt and fillet welded joints located near the lower supporting ring, where the measured temperature was about 350 degrees C. The exhaust system studied has more than 8 m height and the cross sections dimensions vary from 1.5 x 1 m at the inlet section to 2.5 x 2 m at the outlet section, approximately. Its typical service temperatures ranges from 500 degrees C at the inlet section to nearly 200 degrees C at the exit. Based on the stress spectra measured in service and on the fatigue crack growth rates of the material, the paper presents a fatigue life assessment for the exhaust systems studied. The likelihood to occur instantaneous and unstable fracture was also studied and is included in the paper. (C) 2008 Elsevier Ltd. All rights reserved.

作者

我是这篇论文的作者
点击您的名字以认领此论文并将其添加到您的个人资料中。

评论

主要评分

4.7
评分不足

次要评分

新颖性
-
重要性
-
科学严谨性
-
评价这篇论文

推荐

暂无数据
暂无数据