4.7 Article Proceedings Paper

High temperature corrosion in a 65 MW waste to energy plant

期刊

FUEL PROCESSING TECHNOLOGY
卷 88, 期 11-12, 页码 1178-1182

出版社

ELSEVIER SCIENCE BV
DOI: 10.1016/j.fuproc.2007.06.031

关键词

superheater corrosion; waste incineration; PVC; MSW

向作者/读者索取更多资源

Incineration of municipal solid waste is often associated with high temperature corrosion problems. This paper presents results of full-scale corrosion tests in a 65 MW waste fired combined heat and power plant. A failure case indicated alarmingly high corrosion rate of the superheater tubes. Corrosion tests with five different alloys were carried out within this work in order to determine plant specific corrosion rates on different superheater materials. Additional tests were done to determine the effect on the corrosion rate from adding chlorine containing polyvinyl chloride to the ordinary fuel mix. A corrosion probe with metal temperatures ranging from 320 degrees C to 460 degrees C was used to estimate corrosion loss and to collect deposits. The sampling was performed at a flue gas temperature of 470 degrees C for 10 days. The probe rings were analysed using scanning electron microscope and micrometer measurements to determine the deposit chemistry and corrosion rates. The results showed significant differences in corrosion rates depending on tube material. Chlorine was shown to have a key role in the corrosion process, even at these relatively low temperatures. The results indicated a chlorine induced corrosion mechanism involving volatile iron chloride with a high corrosion rate on the superheater materials typically used. Addition of extra polyvinyl chloride to the fuel mix had an increasing effect on the corrosion. (C) 2007 Elsevier B.V. All rights reserved.

作者

我是这篇论文的作者
点击您的名字以认领此论文并将其添加到您的个人资料中。

评论

主要评分

4.7
评分不足

次要评分

新颖性
-
重要性
-
科学严谨性
-
评价这篇论文

推荐

暂无数据
暂无数据