3.8 Proceedings Paper

Seismic analysis of a 2-storey log house

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TRANS TECH PUBLICATIONS LTD
DOI: 10.4028/www.scientific.net/AMR.778.478

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log house; timber; shaking table; seismic performance

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The current paper deals with the analysis of the results yielded by a series of tests performed to evaluate the seismic behaviour of a model log construction. The study was based on an experimental investigation performed to improve the existing knowledge on log houses subject to seismic events. The main part of the experimental work is based on a full scale shaking table test, conducted on a two-storey log house designed by the Portuguese company Rusticasa (R) in compliance with design rules for timber buildings. The test was performed by the University of Minho within the framework of the SERIES Project 'Multi-storey timber buildings' and was coordinated by the University of Trento, at LNEC, Lisbon, Portugal. The geometry of the specimen, the design of the test, the setup and the instrumentation layout are first presented in this paper. The test procedure was conducted in stages with maximum accelerations (bi-directional) of 0.07g, 0.28g and 0.5g. The experimental results of each test have been analyzed and the resultant values of inter-storey drift, wall slippage and uplift measurements, shear deformations and hold-down forces measured are presented. Most importantly, the dynamic properties (fundamental period and mode shapes) of the system have been determined.

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