4.7 Article

Effects of lifted fuel injection using an upstream ramp of a cavity on scramjet combustion

期刊

AEROSPACE SCIENCE AND TECHNOLOGY
卷 142, 期 -, 页码 -

出版社

ELSEVIER FRANCE-EDITIONS SCIENTIFIQUES MEDICALES ELSEVIER
DOI: 10.1016/j.ast.2023.108651

关键词

Scramjet combustor; Cavity; Ramp; Combustion efficiency; Total pressure loss

向作者/读者索取更多资源

This study proposes a scramjet combustor with two ramps and a cavity, and validates its combustion performance through numerical simulations. The results show that the combined effects of the ramps and cavity increase the penetration height of the fuel jet and improve the combustion efficiency.
A scramjet combustor (RSC) incorporating two ramps and a cavity was proposed. The leading edge of the cavity of a normal single-cavity scramjet combustor (SSC) was chamfered downward, and two ramps were arranged on the chamfered surface. Fuel was ejected from the ramp and injected vertically into a supersonic flow. The combustion fields of the RSC and SSC fueled by ethylene at an inlet Mach number of 2 were examined using a validated numerical simulation method. Furthermore, the effects of the lifted fuel injection by the upstream ramp of the cavity in the RSC on scramjet combustion and its mechanisms were analyzed. The combined effects of the chamfered surface and ramp increased the penetration height of the ethylene jet by 48%. This in turn facilitated the ethylene in obtaining oxygen from above and below during the combustion reaction. The low-speed wake region of the ramp was conducive to the successful ignition of ethylene, and the streamwise vortex behind the ramp accelerated the oxygen supply and flame propagation in the lower part of the ethylene jet. The ethylene jet obtained sufficient oxygen from its surroundings to participate in the combustion reaction, and a combustion efficiency of 99% was achieved at the combustor outlet. Compared to the SSC, the RSC achieved a 25% increase in the combustion efficiency and a 2% decrease in the total pressure loss at the combustor outlet. Hence, this study established that lifted fuel injection by the upstream ramp of the cavity can significantly improve the combustion performance of a scramjet combustor. Therefore, further studies and optimization of this novel configuration are required.

作者

我是这篇论文的作者
点击您的名字以认领此论文并将其添加到您的个人资料中。

评论

主要评分

4.7
评分不足

次要评分

新颖性
-
重要性
-
科学严谨性
-
评价这篇论文

推荐

暂无数据
暂无数据