4.6 Article

Design of a Combined Redrawing-Ironing Process to Manufacture a CNG Pressure Vessel Liner

期刊

APPLIED SCIENCES-BASEL
卷 11, 期 18, 页码 -

出版社

MDPI
DOI: 10.3390/app11188295

关键词

D; D; I; (deep drawing and ironing); redrawing-ironing; LDR (limit draw ratio); FEM

资金

  1. National Research Foundation of Korea (NRF) - Korea government (MSIT) [2019R1F1A1058521]
  2. National Research Foundation of Korea [2019R1F1A1058521] Funding Source: Korea Institute of Science & Technology Information (KISTI), National Science & Technology Information Service (NTIS)

向作者/读者索取更多资源

The study proposes a new production method for the second stage using a combined redrawing-ironing die, which can improve efficiency and reduce costs. By adjusting the redrawing-ironing ratio, the forming load, maximum thickness reduction ratio in the second stage, and forming defects in the third stage can be analyzed. This allows for savings in production time and cost by reducing the number of dyes, punch diameter, and processing time in the second stage.
The liner of a compressed natural gas pressure vessel is manufactured by D.D.I. (deep drawing and ironing), which is a continuous process that uses deep drawing to reduce the diameter of a billet and ironing to reduce the thickness of the billet. In the second stage of the existing D.D.I. process, drawing and two steps of ironing have been performed separately with different dies, which requires a long processing time, high manufacturing cost, and installation space. To solve the above problems, this study suggests a new second stage using a combined redrawing-ironing die. A theoretical formula to calculate the forming load of the combined redrawing-ironing process was established and verified with finite element analysis results. The forming load, maximum thickness reduction ratio in the second stage, and forming defects in the third stage were analyzed by varying the redrawing-ironing ratio in the second stage. The results show that the number of dyes (3 -> 1), punch diameter (394.1 mm -> 383 mm), and processing time (39.8 s -> 20 s) in the second stage were obtained to save production time and cost.

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