4.7 Article

Field and three-dimensional finite element investigations of the failure cause and rehabilitation of a composite soil-cement retaining wall

期刊

ENGINEERING FAILURE ANALYSIS
卷 127, 期 -, 页码 -

出版社

PERGAMON-ELSEVIER SCIENCE LTD
DOI: 10.1016/j.engfailanal.2021.105532

关键词

Composite; Excavation; Failure; Finite element; Slope stability; Soil-cement wall

资金

  1. King Mongkut's University of Technology North Bangkok [KMUTNB-61-GOV-D-61]
  2. National Research Council of Thailand (NRCT) [NRCT5RSA63006]
  3. National Research Council of Thailand
  4. Ratchadapisek Sompoch Endowment Fund (2021) , Chulalongkorn University [764002ENV]

向作者/读者索取更多资源

This paper investigates the failure cause of a composite soil-cement retaining wall during reservoir excavation in Bangkok, Thailand, and reports a rehabilitation method, highlighting how insufficient soil explorations led to unexpected soft clay thickness beyond the design range. The rehabilitation involved revising the wall configuration to strengthen the wall against the unexpected soft clay thickness.
In this paper, the failure cause of a composite soil-cement (CSC) retaining wall is examined during reservoir excavation in the soft clay area of Bangkok, Thailand, by field investigation and threedimensional finite element analyses. A rehabilitation method is also reported. The CSC wall consisted of precast reinforced concrete walls, soil-cement walls, and soil-cement columns encased with a stabilized mat. The original CSC wall configuration was designed based on the maximum soft clay thickness of 4 m found in the excavation areas from seven soil boreholes, providing an FSglobal of 1.61. However, a 50-m-long section of the composite wall failed unexpectedly. The field observation revealed that the wall collapsed from the loss of internal wall stability, namely, broken wall structures caused by bending failure. Continuous circular failure was observed due to the shear failure of the surrounding clays. This failure's primary cause was the unexpected soft clay thickness of 7 m induced by insufficient previous soil explorations. Finite element analyses confirmed that the unanticipated 7-m-thick soft clay facilitated significant failure since the FSglobal value was lower than 1.00. The soil and wall bodies exhibited a collapse because the shear and tensile failure points were fully developed in whole soil bodies and wall structures, respectively. Rehabilitation was performed by revising the original CSC wall configuration for supporting 7-m-thick soft clay, namely, increasing the embedded wall structure lengths and soil-cement rows to strengthen the CSC wall. The revised wall configuration improved the FSglobal during excavation to a value of 1.78, resulting in no visual failure after implementing the rehabilitation. During reservoir operation, the water storage level was kept at a level of -1.00 m to obtain a high FSglobal of 2.33.

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