4.6 Article

Upscaling the Zeolite-Anammox Process: Treatment of Anaerobic Digester Filtrate

期刊

WATER
卷 10, 期 11, 页码 -

出版社

MDPI
DOI: 10.3390/w10111553

关键词

wastewater treatment; anammox bacteria; nitrification; zeolite; anaerobic digester filtrate

向作者/读者索取更多资源

State regulatory and other agencies identified that nitrogen loading from the wastewater treatment plants (WWTPs) discharging around its periphery has adversely affected the San Francisco Bay (SFB) water quality. Here we consider the upscaling of the zeolite-anammox process treatment to nitrogen removal from relatively high-ammonia content (similar to 500 NH3-N mg/L) anaerobic-digester (AD) filtrate to facilitate reductions in WWTP nitrogen discharge. First, by operating a 210 L barrel reactor as a trickling filter with a 10% by volume initial bio-zeolite seeding fraction, we found that 6-8 weeks elapsed before the anammox activity became apparent. Moreover, the 10-mm zeolite aggregate reactor achieved an 89% ammonia-N removal compared to the 85% achieved by the 20-mm aggregate. We then evaluated the performance of the trickling-filter design in a 68 m(3) Baker tank nearly filled with 20-mm zeolite aggregate seeded with bio-zeolite at about 1.5% by volume. At an average inflow of 42 m(3)/day, about one year elapsed before achieving adequate anammox activity and acceptable treatment. Unfortunately, inadequate suspended solids pre-treatment of the AD filtrate resulted in clogging problems in the Baker tank reactor, so we evaluated aerobic-anaerobic cycling within the tank and then operated it (anaerobically) as a nitrate-scavenging tank. In the final anaerobic operational stage, nitrate effluent concentrations were <1 mg/L, perhaps due to dissimilatory nitrate reduction to ammonium by the anammox process, but ammonia removal fractions were only about 47%.

作者

我是这篇论文的作者
点击您的名字以认领此论文并将其添加到您的个人资料中。

评论

主要评分

4.6
评分不足

次要评分

新颖性
-
重要性
-
科学严谨性
-
评价这篇论文

推荐

暂无数据
暂无数据