4.8 Article

Evaluating a groundwater supply contamination incident attributed to Marcellus Shale gas development

出版社

NATL ACAD SCIENCES
DOI: 10.1073/pnas.1420279112

关键词

high-volume hydraulic fracturing; shale gas; natural gas; water quality; Marcellus Shale

资金

  1. Leco Corporation
  2. National Science Foundation (NSF) [OCE-11-40159]
  3. Penn State Earth and Environmental Systems Institute
  4. NSF [ANT 1043500]
  5. Division Of Earth Sciences
  6. Directorate For Geosciences [1140159] Funding Source: National Science Foundation

向作者/读者索取更多资源

High-volume hydraulic fracturing (HVHF) has revolutionized the oil and gas industry worldwide but has been accompanied by highly controversial incidents of reported water contamination. For example, groundwater contamination by stray natural gas and spillage of brine and other gas drilling-related fluids is known to occur. However, contamination of shallow potable aquifers by HVHF at depth has never been fully documented. We investigated a case where Marcellus Shale gas wells in Pennsylvania caused inundation of natural gas and foam in initially potable groundwater used by several households. With comprehensive 2D gas chromatography coupled to time-of-flight mass spectrometry (GCxGC-TOFMS), an unresolved complex mixture of organic compounds was identified in the aquifer. Similar signatures were also observed in flowback from Marcellus Shale gas wells. A compound identified in flowback, 2-n-Butoxyethanol, was also positively identified in one of the foaming drinking water wells at nanogram-per-liter concentrations. The most likely explanation of the incident is that stray natural gas and drilling or HF compounds were driven similar to 1-3 km along shallow to intermediate depth fractures to the aquifer used as a potable water source. Part of the problem may have been wastewaters from a pit leak reported at the nearest gas well pad-the only nearby pad where wells were hydraulically fractured before the contamination incident. If samples of drilling, pit, and HVHF fluids had been available, GCxGC-TOFMS might have fingerprinted the contamination source. Such evaluations would contribute significantly to better management practices as the shale gas industry expands worldwide.

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