4.8 Article

Combined Nitritation-Anammox: Advances in Understanding Process Stability

Journal

ENVIRONMENTAL SCIENCE & TECHNOLOGY
Volume 45, Issue 22, Pages 9735-9742

Publisher

AMER CHEMICAL SOC
DOI: 10.1021/es202181v

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Efficient nitrogen removal from wastewater containing high concentrations of ammonium but little organic substrate has recently been demonstrated by several full-scale applications of the combined nitritation-anammox process. While the process efficiency is in most cases very good, process instabilities have been observed to result in temporary process failures. In the current study, conditions resulting in instability and strategies to regain efficient operation were evaluated. First, data from full-scale operation is presented, showing a sudden partial loss of activity followed by recovery within less than 1 month. Results from laboratory-scale experiments indicate that these dynamics observed in full scale can be caused by partial inhibition of the ammonia oxidizing bacteria (AOB), while anammox inhibition is a secondary effect due to temporarily reduced O(2) depletion. Complete anammox inhibition is observed at 0.2 mg O(2)center dot L(-1), resulting in NO(2)(-) accumulation. However, this inhibition of anammox is reversible within minutes after O(2) depletion. Thus, variable AOB activity was identified as the key to reactor stability. With appropriate interpretation of the online NH(4)(+) signal, accumulation of NO(2)(-) can be detected indirectly and used to signal an imbalance of O(2) supply and AOB activity (no suitable online NO(2)(-) electrode is currently available). Second, increased abundance of nitrite-oxidizing bacteria (NOB; competing with anammox for NO(2)(-)) is known as another cause of instability. Based on a comparison of parallel full-scale reactors, it is suggested that an infrequent and short-term increased O(2) supply (e.g., for maintenance of aerators) that exceeds prompt depletion of oxygen by AOB may have caused increased NOB abundance. The volumetric air supply as a proxy for O(2) supply thus needs to be linked to AOB activity. Further, NOB can be washed out of the system during regular operation if the system is operated at a sludge age in the range of 45 days and by controlling the air supply according to the NO(3)(-) concentration in the treated effluent. Early detection of growing NOB abundance while the population is still low can help guide process operation and it is suggested that molecular methods of quantifying NOB abundance should be tested.

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