4.5 Article

Experimental study of a degradable polymer drilling fluid system for coalbed methane well

Journal

JOURNAL OF PETROLEUM SCIENCE AND ENGINEERING
Volume 178, Issue -, Pages 678-690

Publisher

ELSEVIER SCIENCE BV
DOI: 10.1016/j.petrol.2019.03.065

Keywords

Degradable polymer drilling fluid; Bio-enzymes; Permeability recovery; Polymer removal; Coal cuttings carrying; South Qinshui Basin

Funding

  1. National Science and Technology Major Project of China [2016ZX05067001-007, 2016ZX05041002-002]
  2. Shanxi Coal-based Scientific and Technological Key Project of China [MQ2014-04]
  3. Opening Foundation of Key Laboratory of Tectonics and Petroleum Resources (China University of Geosciences), Ministry of Education of China [TPR-2017-18]

Ask authors/readers for more resources

Drilling along the coal seam is an effective way to improve gas recovery. Due to complex coal body structure and natural fractures, there are many difficulties, including a low abilities of cutting carrying, leakage while crossing the fracture zone and reservoir damage. In this work, a low density degradable polymer drilling fluid system is developed to solve these difficulties to enhance coalbed methane (CBM) production. In the laboratory, the properties of the polymer drilling fluid were evaluated using the coal cuttings suspension experiment, borehole stability simulation test, viscosity attenuation method, laser particle size analysis, polymer removal and core permeability recovery method. The experimental result indicates that the developed drilling fluid has good rheology and filtration, a high yield point and a strong inhibition, thereby meeting conventional drilling requirements and carrying coal cuttings effectively. Under the bio-enzymes, the viscosity of degradable drilling fluid can be initially reduced to 16%. The optimum temperature and pH for the enzyme activity is obtained, and enzymes with small weight fraction of 0.01% can dramatically alter rheological properties of drilling fluid and thereby the high biological activity. After degradation, the particle size in drilling fluid decreases greatly. During immersion test, the polymer film on the surface of the lump coal and thin sections is almost removed by enzyme solution. The reservoir's permeability damage rate may be reduced from 50% to 25% via the functionality of the enzymes, and it is noticeable that the relationships between effective stress and gas permeability treated by the drilling fluid and enzyme still obey the exponential function. Field applications show that the drilling fluid has a good coal fines resistance and compatibility with conventional plugging materials, which ensures the long horizontal footage of 901 m with the short construction period. The later decreased viscosity of the drilling fluid by the enzymes is conducive to reduce the damage to the coal reservoirs.

Authors

I am an author on this paper
Click your name to claim this paper and add it to your profile.

Reviews

Primary Rating

4.5
Not enough ratings

Secondary Ratings

Novelty
-
Significance
-
Scientific rigor
-
Rate this paper

Recommended

No Data Available
No Data Available