4.3 Article

Crash performance of strong-post W-beam guardrail with missing blockouts

Journal

INTERNATIONAL JOURNAL OF CRASHWORTHINESS
Volume 17, Issue 1, Pages 93-103

Publisher

TAYLOR & FRANCIS LTD
DOI: 10.1080/13588265.2011.626931

Keywords

guardrail; blockout; pendulum; Finite Element Model; rupture

Funding

  1. National Cooperative Highway Research Program (NCHRP) [22-23]

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Missing blockouts in a strong-post w-beam guardrail, a condition most commonly associated with environmental decay or crash damage, has never been thoroughly investigated. To determine the risks posed by the removal of a blockout, a combination of component-level pendulum testing and full-scale finite element models of crash tests was used to assess whether a missing blockout renders the guardrail performance unacceptable. Finite element models were developed for three pendulum tests. (1) A 30.1-kph impact into a test installation with proper blockout installation resulting in containment, (2) a 30.5-kph impact into a test installation with one missing blockout resulting in splice rupture, and (3) a 26.7-kph impact into a test installation with one missing blockout resulting in containment. The finite element model was able to reproduce the splice failure in test 2 when the appropriate mesh quality and failure criteria were used. Full-scale crash test models of a 2000-kg pickup truck striking a 29 post guardrail at 25 degrees were developed. The simulation results indicated that wheel snagging was not a major problem. Although a missing blockout increases the maximum rail tension and deflection by as much as 13%, such guardrails are still capable of safely redirecting of vehicles.

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